Hi all,
I thought I had a thread about this from last fall, but I can’t find it so here’s a new one with an update.
I have an 1984 Oday 26 with a 1GM. Last fall, after putting the boat on the hard, I pumped out the fuel tank as best I could. I removed about 13 gallons of some really ugly looking diesel. I replaced it with 10 gallons of new. I didn’t add any fuel treatment because I figured the new fuel would have enough to get me through the winter and I’d add some this next fall.
in short, I thought if I removed to old fuel and added new fuel I’d do no harm.
so….this spring I hook up water, bleed the fuel system and run the engine for 15 minutes. It runs fine.
the next day I put the boat in the water and run the engine another 15 minutes. It runs fine.
a couple of days later, in order to put up the furling jib on a super windy day we reposition the boat to a slip into wind and it runs fine.
the day before yesterday we go sailing and use the motor about 15 minutes with no issues. After a great sail I fire up the motor, take down the main, furl the jib and motor in. Entering the marina the motor stops. It didn’t it show any unusual symptoms, it simply stopped as if I pulled the fuel knob.
I yank out jib and sail through the marina to the slip. Other than some yelling at a pontoon boat it went without incident.
the next day I pull and change both filters which look clean.
in the process, I find the tank filter housing full of fuel. The filter housing on the engine is empty. Obviously, some air got into the system somehow but everything seems tight. I bleed the air out of the system and start the engine. I run it for 30 minutes, in gear and it runs perfect. Today I went back to the boat and inspected the fuel vent and ran the engine in gear at 1500rpms for another 30 minutes with no issues. I found no leaks.
any thoughts on why it might have failed at just about the worse possible moment?